2 x GI-7B 432 MHz
amplifier project
This
project had three goals. First was to get more power out on 432 for EME
and extended tropo work. Second was to learn more about the GI-7B
russian triode. Third was to learn more about UHF stripline amplifier
construction techniques. It turned out that this was the most difficult
tube type power amplifier project I have attempted to date.
The project started when several GI-7B russian triodes were obtained. A
study of designs available on the internet led to the conclusion that
the SP5CIC design would be the easiest to build. This design was
documented on the ND2X QRO web page. In retrospect that conclusion was
incorrect. But after the sheet metal parts were fabricated, I was
committed.
The chassis was fabricated mostly from scrap aluminum sheet. I used
store bought 1/2 x 1/2 x 0.05 aluminum angle to hold the sides
together. There are about 300 4-40 holes drilled and tapped in this
thing! The anode line was fabricated from copper sheet 0.032 thick
obtained from McMaster-Carr as were the hundreds of 4-40 screws.
The anode compartment was pretty straightforward:

A sheet of .032 aluminum was drilled for the 4-40 screws around the
outside edges first. Next the tubes were located and holes drilled and
reamed to provide a snug fit around the grid flanges. Then the many
holes for cooling were drilled. After finishing the plate, the tubes
were held down with aluminum clamps.
Next step was to fab the anode resonator. It was pretty complex as it
needed to have slots which matched up with the anode cooler fins. Here
it is in place before the coolers are installed:

Here are shown the coolers installed:

When I started to fab the cathode line, I found the first of many
problems with this design. There was no way I could connect the
resonator to the cathodes of the tubes. I played with some finger stock
but was not happy with that. I eventually wound up using the YU1AW
technique of matching with discreet components. This is a photo
of the completed cathode compartment:

Left center are the filament chokes. Just to the right of the chokes is
the cathode matching network comprised of two small piston trimmer caps
and a small inductor. The dark strip in the center is just a piece of
black tape covering some unused holes. Next to that is the
cathode bias circuit which provides the necessary 30 or so volts bias.
Next right is the anode tuning mechanism which pulls down on the
flapper cap.
After the cathode compartment was sorted out, I tried tuning up the
anode compartment with my network analyzer and found it was way out of
band. A slight tweak of the anode resonator length got everything to
tune OK but it was later discovered that the line length was correct
and the "flappers" (tune cap and load cap) needed to be shortened
instead.
When power was finally apply, the power output was much lower than
hoped for and there was a lot of thermal drift. All this made it
unusable for EME service. To make a very long story somewhat shorter, I
discovered that there were a number of problems contributing to the
poor performance.
The first problem I found was anode resonator efficiency. The SM5BSZ web page
(http://www.sm5bsz.com/power.htm) was very helpful for trouble
shooting the anode resonator and Leif was very helpful with suggestions
for improving efficiency. Unfortunately the mechanical aspects of this
design prevented me from implementing the best of Leif's suggestions. I
was able to drop the tank loss from almost 20% down to under 14%. Here
is the modified tune flapper cap:

Tube mismatch was suspected to be an issue so I built a tube tester
from a cardboard box:

While running grid voltage vs. anode current curves at very reduced
anode voltages, I quickly found out that I was not running nearly
enough air through the anode coolers to keep the tubes at a reasonable
temperature. The claims from people running 400 watts out with nothing
but a muffin fan for cooling is pure BS! These tubes need around four
times the air flow that a 4CX250B needs for the same dissipation due to
the poor efficiency of the anode cooler.
OK, with more air I got some curves and discovered that I had
inadvertently selected the two most mismatched tubes I had! The two
closest were re-installed in the chassis and a painful mechanical
re-build to get more air was undertaken. My initial design used a low
profile squirrel cage blower mounted on the side of the chassis
providing a nice clean low profile. It pressurized the cathode
compartment and air was routed up to the anodes through holes drilled
in the base plate. See the above photos. Now I had a much larger blower
mounted on the top cover and pressurizing the anode compartment. Some
air was allowed to route down to keep the filament pins cool.
During re-assembly a slight unbalance in the cathode matching network
was discovered which caused a small drive imbalance. This was corrected
and the amp was tried again. With all the above mods in place, I was
able to run at a reasonable power output with reasonable efficiency,
and manageable thermal drift. I can now run EME duty cycle with now
re-tuning required during a sequence.
Here are some photos of the final configuration, keep in mind that it
looked somewhat better before all the mods:

The shaft
you see has a cam wheel on the far end which pushes against the load
flapper cap for adjustment.




Performance is as follows:
Anode voltage = 1950 under load
Anode current = approx. 550 ma.
Power output = 550 watts (more possible but not without thermal drift)
Drive power = approx. 30 watts
Note the power output is key down CW brick on key, not SSB PEP BS power.
I missed some of my goals on this project due to poor information
obtained on the web. I had to discover for myself the limitations of
these tubes. With the knowledge I have gained on this project, I feel
like I can do better next time around. Compared to building HF and low
VHF amps, this was very difficult. The dimensional tolerances required
are significantly closer than any G-G linear amplifier I had built
before. I'm used to doing microwave stuff in a full commercial lab with
full machine shop facilities handy. Doing this stuff at home is less
fun than I like. I'm really not sure if I'll ever try a UHF project of
this sort again.